Thursday 01.28.10

First Warm Up

Got things fixed and I’m thinking I’m nearly ready for a ride! The Schooner started right up. As I let it warm up I watched for any sign of trouble.  Things seemed pretty good: voltage was right, engine temp nominal, no funny noises.  I started thinking everything was right.

Snif— what’s that? Snif-snif— smoke? The engine cover is still off and smoke started pouring in from the starboard exhaust.

At first, I thought maybe it was just spilled oil burning off the exhaust manifold, but as the engine warmed it got worse.  I’m thinking it should have burned off and started looking around. Found a split transmission line squirting fluid on the exhaust manifold— what a fireball that could have made going down the road!!

Shut ‘er down and dropped a pan underneath to catch the fluid.

After cooling, I looked around underneath.  A bolt was missing from the union where the exhaust pipe attaches to the manifold. It had only moved sideways about an inch, but it was enough to touch a transmission cooling line. No telling how long the exhaust had been like that.  I had fixed it once in 2002— about 8 years and 3,000 miles ago.  Apparently it had rubbed, and when I jostled the lines fixing the radiator and the starter, that was enough to open the breech.

Dang.  More lines to fix…

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01.26.10

Busted Solenoid Terminal

Starter with busted Solenoid

For a long time, there has been an intermittent starter problem.  I first had it when driving to my mother’s funeral in AZ in 97.  I ran some new wires to the solenoid and seemed to take care of the issue for a long time— until this fall.

When I arrived back in Sanford last November, I bought a battery, put it in, and the old Prairie Schooner fired up like she’d been running yesterday.  Then when I turned it off, it wouldn’t start again until I wiggled the wires near the battery.

Then it did it again— only wiggling the battery wires didn’t help, but fussing with others did.  It was maddening and I figured I’d better get to the bottom of it while I had everything opened up and the right front wheel off.

Getting the starter back on the engine was work, but changing the solenoid on the starter took about 10 minutes.

Discovered that the cable terminal on the starter was loose.  The nut was difficult to get at, so with a little snub box end wrench I tightened it.  When I tried to give it one more ‘umph’, the terminal post snapped right off the starter.

When I took the starter out, the end of the battery cable broke off.  The starter is right below the exhaust manifold.  Apparently, the cable end had gotten hot a few times.  Bottom line: needed a new cable and a solenoid.

The local auto-electric place had the solenoid for $15.  Advance had a cable for another $15. Since I was trying to make sure I wouldn’t have any more trouble, I replaced the old wire that ran up to the dash as well. I want all nice new connections.

And hey, let’s leave as little to chance as possible here.  I took the negative cables off and sanded the connections— the schooner has 2: 1 to the frame, 1 right to the starter bolt.

Good to go!

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01.25.10

Adding Fluid to Reservoir

Click for demonstration

Pairie Schooner uses HWH 'kick-down' leveling jacks

The reservoir that holds the hydraulic fluid for the HWH kick-down house jacks needed to be topped off. The HWH jacks were an after market addition— and a good one!  I wouldn’t want to have an RV without some sort of leveling system.

The HWH system was added in 1997.  Camping World had a special offering the jacks with free installation.  Don’t know if they still do that, but it was a good deal— in fact,they run similar deals all the time (I bought Bilsteen shocks installed for less then other places sold lesser quality shocks and an Air Lift kit installed free). It has worked well and been very reliable.

One of the best things about the leveling jacks is that it opens up a large range of parking possibilities.  The ground can be quite unleveled— either side to side, or front to back (or both) and the jacks can set the chassis level.

The leveling capability has let me park in lovely locations that would normally never be used for camping.

Once leveled, the coach also becomes very stable and does not rock when you move around inside.

There are other benefits to having leveling jacks, not the least of which is being about to lift the coach and change tires.

The leveling jacks don’t require much maintenance, but there is some.  The main thing I do is spray the hydraulic cylinders with silicon lubricant to keep them from rusting and tearing up the seals.  The other thing is checking the fluid level in the reservoir. The HWH levelers were an after market add-on.

HWH only uses transmission fluid (not hydraulic oil)

The only real deficiency is that the reservoir for the jacks is tucked up in the frame and the filler cap is difficult to get to.  Didn’t want to cut a hole in the floor, so I drilled a small hole in the hull so I could run a long funnel tube to the fill hole.  That has worked well.  And I can fill it without having to lay under the coach.

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01.24.10

Tires

Felt good to finally be getting the tires back on!

I’ve never driven the Schooner enough to run the tread off the tires.  The tires ‘dry-rot’ first.

To deal with the eventual dry-rot, I just buy 2 new tires for the front.  I rotate the previous front tires to the inside rear.  The oldest tires go on the outside rear where they are easiest to change.

At some point, an outside rear tire will need replacing, and when it does, I go buy 2 new ones for the front and rotate again.  This keeps my front tires fresh.

I always want to have good tires on the front.  A front blow-out can be traumatic— even deadly.  A rear tire blowing is much less of a problem because they are duals and there is no loss of control.

Changing 2 tires is much less expensive than buying 6.  And because I only replace the front tires and it costs less than replacing all 6, I tend to do it more often.  Something about always having new tires on the front that feels good.

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Brakes are done. Radiator is ready to go back in.

01.23.10

From the Bottom!

The only way the radiator would go back in was from the bottom.  That meant lifting the front quite high in the air.  Still it was tight and I wanted to be careful not to damage the cooling fins or knock a hole in it.

Radiator in position to be raised

I positioned the radiator under the chassis where I could use a floor jack with a block on top to raise the radiator up to where it had to be to get the mounts put back on.

Before getting the radiator back in place, I had to put the pulley, belts, and fan blade back on, and then position the fan cowling back in place. The cowling attaches to the radiator, but there isn’t room to get it back in once the radiator is in place.

HELP! Got me by the head!!

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Belts on. Top of radiator bottom

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Fan cowling set in place

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Radiator back in position

With the radiator back in position, the cowling was attached.  Next all the brackets, braces, and hoses were put back on.  Then I had to cut and fit the new ends of the transmission cooling lines and the radiator was done.

The last thing to do on the front of the radiator was to put the engine oil cooler back on.

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01.22.10

Bleeding Technique

Bleeding the brake linesUsually, brake bleeding is a 2 person job.  I’ve also seen special tools with vacuum pumps for bleeding solo.  I use a simpler technique.

I made the end of a piece of tubing rigid with a piece of rod.  That way it would stay pointed down in the bottom of a container with brake fluid in it.  The other end I put on the bleeder on the caliper. When the brake is pressed, the air bubbles and brake fluid are pumped into the container.  The oil bath at the bottom lets the air bubbles escape, but only fluid can get sucked back up the hose.

I start with the furthest brake and work toward the one closest to the master cylinder.  The excess brake fluid is recaptured in the container.  This technique might use a little more fluid, but it gets it done without a second set of hands.

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Radiator is a monster. Needed to find the hoses before reinstalling it.

Radiator R&R

Sent the radiator out for R&R. The radiator is a monster— must be 100 lb or more. Old fellow in Spring Lake, NC (Spring Lake Radiator Service) did a good job. Said it had 2 small leaks and was very dirty. He repaired it, cleaned it, and painted it. Cost $50.

Radiator Hoses

One of Robert’s Rules of Repair states: Never cause more work than you are getting done.

Originally, replacing the radiator hoses seemed like a prudent thing to do whenever you go through this much trouble. What I hadn’t counted on was that the radiator hoses for my engine/chasis combination is not available. I searched and searched. Something else might work for the upper hose, but the lower hose must fit precisely around the front pulley and lay behind the belts before going under the cross frame and up to the bottom of the radiator.

Had to fabricate a hose out of pieces of other hoses. It's probably the most expensive radiator hose ever. Sure hope it lasts!

The old lower radiator hose wasn’t bad and could have been reused, except that I cut it to get the radiator out.  So even though I couldn’t get one, it had to be replaced.

So my only real option was to make something.  I did a lot of running around comparing hoses trying to find the right bends.  I bought several from different stores.  After I selected 3 I could use I was able to take the others back.  The photo shows that I still had difficulty trying to match the exact bends.  However, some of the bends weren’t so critical, but the one that ran around the front pulley could only  go in one way.

Because the radiator is so large and the fit with the fan cowling so tight, there was no way to run the lower hose directly to the radiator— it had to go underneath the cross frame.

Next I had to find some pipe to make couplings out of.  Wanted to use copper, but didn’t find any.  Settled for galvanized.

Well, cutting the radiator lines to get the radiator out turned into just about as much work as the brake lines and a heck of a lot more running around! I’ve got the radiator prepped, but I don’t want to put it back in until I’m certain that the brakes fixed (don’t want to be taking it out again).

Transmission Cooling Lines

Another set back was that I had to cut the transmission cooling lines that ran to the radiator to get the radiator out.

In the photo at right, you can see one of the brass couplings ready for a new end to run into the radiator.  I’ll match the bends to the old pieces, then cut them to length and fit them after the radiator is back in place.

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Hidden brake leak in the cross frame between the engine and the radiator.

01.13.10

Brake Line Repairs

After letting the Prairie Schooner sit for 5 years, I knew there would be problems. The fun part, of course, is finding them.

I found brake fluid pouring out between the engine and the radiator up in the cross frame.  No mater what angle I tried to use, I just couldn’t see the exact spot— let alone effect a repair.

Disassembling the front of the engine to get at the cross frame from the top. The radiator had to come out through the bottom! That meant jacking the RV up frighteningly high.

The only solution was taking the radiator out and getting at it from the top through the front.  I checked on the internet for a recommended way of getting it out.  Advice: don’t do it!  Well, that wasn’t an option for me.

The radiator had to come out through the bottom.  Nothing is easy— the transmission lines didn’t want to come off, so I had to cut them— and I cut the old hose off the bottom too.  What the heck?  Good to change the hoses anyway.  Right?

Next I had to raise the Schooner up high and drop the radiator out through the bottom.  As long as it was out, I dropped it off at a radiator shop for cleaning and repair— it looked pretty dirty.

The brake line still wasn't easy to reach, but it was accessible. Sometime during the life of the brake line, it had gotten bent. Right where the metal was fatigued, it failed.

I was finally able to see the problem: a line with a hole in it.  The rest of the ling looked good, but the bad part had gotten bent at some point and that’s where it fatigued. I cut out the bad section and replaced it.

Joining the new piece of line with the existing line requires a double flair compression fitting.  A double flair is a double bend on the end of the line that makes for a much stronger ‘lip’.  As you might guess, there is a tool for it called a double-flairing tool.

Having gotten that taken care of, I put a paper towel under the line to show me if there are any leaks or wetness, then I bled the lines and mashed the brake pedal.  I pushed harder than I ever have while driving— and when I did, something let go.

I matched the bends with the portion of the brake line I removed. The exposed ends needed double flares. I put the new piece in and checked for leakes.

OK.  Better here than on the road.  I had to crawl around underneath to find the break.  The drip was coming from a bend in the line up over the starboard (right) rear shock.  I picked a point farther forward and cut the line where it looked like it wouldn’t be too difficult to get the flaring tool up in there.

Bought a long piece of line, matched the bends with a bending tool, then cut the length to match and double flared the end.

Did a good job matching the bends and the new piece fit back in quite nicely.  Getting a double flare on the end of the existing piece to 2 attempts to get straight.

Dang! Something popped and I had to crawl around and find it. Well, better to happen now than chugging down a mountain or something!

When I tried to bleed my new line, nothing came out.  Right away I knew what that meant: the flex hose had collapsed inside.  It’s a common problem.  This Chevy P-30 has 5 places where flexible brake hose is used, 3 had already been replaced.  Sometimes the collapse will cause a brake to lock up, and sometimes it will cause it not to work.

Well, no sense not to change them both.  Problem is, the rear flex lines were hard to find!  All the other flex lines for the brakes can be had from placed like AutoZone for around $15. What I discovered was, even though the P-30 is one of the most common truck chassis in the world, for only 2 year disc brakes were used on the back: 1978 & 1979.  I tried to have some made, but the hydraulic guys couldn’t get the right banjos.

The back flex hoses were hard to find and very expensive, but I needed them.

NAPA was finally able to run them down for me from a warehouse in IL.  Price: $100/pair.  Ouch!  The front banjos are the same, but the hoses are different, I may have been able to fashion something by changing the ends on a pair of front flex lines, but after all was said and done, I probably would have spent just as much. Plus, getting the ordered hoses gets it done right for sure.

What I decided after going through all this is if I were doing it again, I wouldn’t cut and replace a section of brake line.  It worked ok, and it’s safe that way, but the lengths of line are cheap, and laying on my back with brake fluid dripping in my face while using a flaring tool was a bitch.  Instead, if I do it again, I will go all the way back to an existing union in the line and rejoin it there.  That way, I can match the bends, cut it to length, and flare the ends all on the bench— underneath I won’t need to fool around with a flaring tool in tight quarters.  Another plus is that more of the line is new and there is one less double flare to make.

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